钻采工艺 ›› 2022, Vol. 45 ›› Issue (3): 141-145.DOI: 10.3969/J. ISSN.1006-768X.2022.03.26

• 生产线上 • 上一篇    下一篇

“三低”气田放喷回收工艺在苏里格气田的应用

胡朋伟1,唐婧2,薄婷婷3,王志恒3,李鹏3   

  1. 1中国石油长庆油田苏里格气田开发分公司 2中国石油长庆油田公司咨询中心 3中国石油长庆油田公司第四采气厂
  • 出版日期:2022-05-25 发布日期:2022-06-28
  • 作者简介:胡朋伟(1989-),工程师,学士,主要从事天然气开发技术工艺研究。
  • 基金资助:
    国家科技重大专项“鄂尔多斯盆地大型低渗透岩性地层油气藏开发示范工程”(编号:2016ZX05050)。 

Research and Application of Natural Gas Recovery Process in "Three Low"Gas Field in Sulige Gas Filed

HU Pengwei1, TANG Jing2, BO Tingting3, WANG Zhiheng3, LI Peng3   

  1. 1.Sulige Gas Field Development Company of CNPC Changqing Oilfield, Xi’an, Shaanxi 710018,China; 2.CNPC Changqing Oilfield Company Consulting Center, Xi’an, Shaanxi 710018, China; 3.The Fourth Gas Production Plant of CNPC Changqing Oilfield Company, Xi’an, Shaanxi 710018, China
  • Online:2022-05-25 Published:2022-06-28

摘要: 苏里格是典型的低压、低产、低丰度“三低”气田,在开发过程中,必须对储层进行压裂试气,压裂完成后, 需要采用放喷流程进行放喷排液、试气求产,在试气排液期间,通过点火的方式对排放出来的天然气进行燃烧处 理,一定程度上造成资源浪费和二氧化碳等温室气体排放。为此,在试气过程中,设计并应用“湿气收集﹢高压分离﹢天然气回收”的放喷天然气回收工艺,对现场33口井进行天然气回收,同时分析了不同类型气井运行的各项参数,达到了天然气回收的目的。该工艺能够较好的处理排液初期的混合物,分离天然气达到进站集输的条件;在水平井和直定井运行效果均较好,水平井具有更好的经济效益;能够大量减少试气放喷二氧化碳排放并且有效满足苏里格气田不同井型试气放喷天然气的回收,实现较好的经济和环保效益。

关键词: 气液分离, 放喷气回收, 除砂, 二氧化碳, 经济效益

Abstract:

Sulige Gas Field is a typical "three low" gas field with low pressure, low production and low abundance. During the development process, the reservoir must be fractured and tested for gas. After fracturing, the discharge flow is used to test the gas production. During the gas production test, the discharge natural gas is burned by ignition, which causes the waste of resources and the emission of CO2 and other greenhouse gases emissions to a certain extent.Therefore, in the process of gas test, the gas recovery process of moisture collection, high pressure separation and natural gas recovery was innovatively designed and applied to recover natural gas from 33 Wells on site, and the operation parameters of different types of gas Wells were analyzed, achieving the purpose of natural gas recovery.The process can better deal with the mixture at the initial stage of drainage, and the separation of natural gas can reach the conditions of gathering and transporting in the station. The operation effect in horizontal well and vertical well are both better, horizontal well has much better economic benefit. The CO2 emission from test gas injection can be greatly reduced and efficiently meet the recovery of different well types of test gas injection in Sulige gas field, achieving better economic and environmental benefits. 

Key words: gas-liquid separation, discharge gas recovery, desanding, carbon dioxide, economic benefit